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Author: Subject: help splitting r1 case
jlayton

posted on 14/6/15 at 02:29 PM Reply With Quote
help splitting r1 case

as above really. i need help splitting the crankcase as I have melted 3 pistons iv took head off first to see what damage I had. so now I need to split the crank case, iv managed to undo what I think is everything, and the case is split the hole way across apart from the last 1cm rotor side. do I need to take the rotor off is that my problem?? like I say the case is off apart from this

many thanks

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rusty nuts

posted on 14/6/15 at 05:07 PM Reply With Quote
Haven't worked on any bike engines since the 70s but I would have thought you would have to remove the rotor and any internal backplate before you can seperate the crankcases
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CosKev3

posted on 14/6/15 at 06:43 PM Reply With Quote
Pretty sure the stator thing inside the rotor is bolted to both halves of the casing.
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jlayton

posted on 14/6/15 at 07:25 PM Reply With Quote
thanks for your comments. but just found many cracks across the valves on the head so would not be surprised if the bores are cracked also as it got that hot it melted 3 pistons. think I need a new engine
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sdh2903

posted on 14/6/15 at 07:50 PM Reply With Quote
Any ideas what caused the failure?
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jlayton

posted on 14/6/15 at 08:08 PM Reply With Quote
I turbo'd it on completely std internals at 8 psi so yeah my own fault. but it lasted 4 hours on the rollers sweet as a nut. the thing on my mind is when it started running rough I thought id check the plugs, to my amazement they was not even hand tight (I mean really loose) and the washer on the plugs was not even squashed from new? would this of caused it to get 2 hot?
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mark chandler

posted on 14/6/15 at 08:50 PM Reply With Quote
loose plugs should not make it run hot.

Standard internals should be able to hold 8psi, it must have been running weak if you did not hear any pinking.

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jlayton

posted on 14/6/15 at 09:02 PM Reply With Quote
What you mean running weak? (I had it set up by pdq straight away) so I thought it would be running ok he said he set it up for 12.8 afr. Would it be because I never touched the ignition timing? I really don't no what caused it to get that hot and would love to no. And never herd any noise ( what's linking)
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mark chandler

posted on 14/6/15 at 09:51 PM Reply With Quote
Pinking is the engine knocking because of pre-ignition, high pitched rattling sound.

12.8 is rich so that's not the cause unless it's something related such as the fuel pressure regulator failing or low fuel pressure making it run lean and burning it up, when it was on the rollers he would have alerted you if it was pinking then.

Once you get it back together I suggest you get a wide band sensor and watch it like a hawk, my blade engine has been thrashed for many hours around various tracks on standard internals.

When it went bang I am guess you were on light throttle as giving it the beans quickly builds the speed up, do you know what the AFR was at 1/4 throttle?

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jlayton

posted on 14/6/15 at 10:07 PM Reply With Quote
To be honnest I have a aem wideband fitted . But when in the rollers he said my wb was reading different to his? And he said it could of been where I had positioned it. So never really kept a close eye on it to be honnest. When it played up I took my friend out, Guv it loads like you do then took his dad out and when I backed off for the last time as we was almost home I noticed it was missing (sounded like it was on 3 cyclinders) stopped and it blow the d shape rocker cover open like a door and chucked about 300mil of oil out. Like I say would love to no what caused it as going to build a forged engine and don't want the same to happen. Any advice tips would be great
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mark chandler

posted on 14/6/15 at 10:35 PM Reply With Quote
Consider easy things to start off with

was it low on fuel with an unbaffled tank?

Have a look at the fuel filter, is it blocked?

Failing FPR

Over boosting to do with the Vacumm tubes dropping off keeping the wastegate closed (did it feel exceptionally fast just before going bang, I have an overboost cutout configured which has saved me a couple of times).

Really anything that could cause it to run weak, it may only take a few seconds to start damaging things, as three Pistons out of 4 are stuffed it has to be something generic.

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CosKev3

posted on 15/6/15 at 03:36 AM Reply With Quote
Was it anything to do with the thread you put up about the slides in throttle bodies not opening fully?

I personally think if the tuner said the power was the same at 80% throttle as it was at WOT it wasn't totally set up correctly, either boost control or fueling/air flow had issues.
I would have hoped they would have detuned it and told you it had issues that needed sorting before running it flat out on the road?

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jlayton

posted on 15/6/15 at 06:11 AM Reply With Quote
Just a thought I have a torques fpr rising rate 1:1 new cost me 149 pound. I think it was a 50 psi before it was tuned and he never touched it so maybe the std fuel pump can't flow enough? As I have herd the fuel pump a few times sounding like it's working hard? And some times it was at 9 psi when held wide open
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mark chandler

posted on 15/6/15 at 06:42 AM Reply With Quote
That's your problem, it should be 50psi at full chat, I run a v12 jaguar pump on mine as it can flow loads of fuel and has nice barbed fittings.

You leaned out and burnt it out.

I would be looking at a straight engine replacement, forget forged parts for now, replace the pump and fit a corse filter between the tank and pump and a big injection filter between the pump and engine, mine is off a 928 Porsche so I know it can again flow a lot.

Also check fuel lines, they may be collapsing between the tank and pump + the pickup could be blocked (the pump should not be changing its noise much, sounds like a blockage or knackered)

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gaz_gaz

posted on 15/6/15 at 08:24 AM Reply With Quote
As mark says. Fuel pressure/supply problem.
I'd also go for a stocker 5pw. Mine coped fine with 7psi.

PDQ are very very good and have set up 2 of my BECs but they where both N/A.

Do yourself a favour and speak to Sean at Bigcc racing in Wokingham if you need a turbo bike engine tuned. They have a car dyno and anything those boys don't know about boosted bikes isn't worth knowing.

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jlayton

posted on 15/6/15 at 09:09 AM Reply With Quote
Cheers for the info I have the stock pump in the bottom of my tank so do I need a upgraded direct replacement to go in the tank, as I don't no how to go about it
Thanks again

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jlayton

posted on 15/6/15 at 09:17 AM Reply With Quote
Is there anyway I can check that my fpr is good even tho I can't start the car as the engines out? Just so I can iliminate that
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gaz_gaz

posted on 15/6/15 at 09:24 AM Reply With Quote
I used an external bosch 044 pump.
Some use the Walbro 255ltr/hr pump which is commonly used on jap car tuning

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dave_424

posted on 15/6/15 at 09:32 AM Reply With Quote
I would say that 12.8 is too lean on an engine that you are running close to the limit. 11.5 would be much safer.

Fuel pressure should be 3 bar/43.5 psi at idle and it should increase when your boost increases, so at 10psi boost, fuel pressure should be 53.5psi

Adding the ability to control ignition timing will definitely help you save your engine.


To check the FPR, connect the FPR to throttle bodies and connect the return line, just like it's plumbed to run the engine. Then run the pump, check fuel pressure. Then using a blowgun from a compressor, apply pressure to the vac port on the FPR (Careful, don't blast 150psi down it). Set your compressor reg to 10-20psi, when you apply this pressure to the vac port, you should see fuel pressure rise the same amount.

Another vote for BigCC racing, doesn't sound like your tuner got everything sorted or explained everything to you.

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mark chandler

posted on 15/6/15 at 09:43 AM Reply With Quote
quote:
Originally posted by jlayton
Is there anyway I can check that my fpr is good even tho I can't start the car as the engines out? Just so I can iliminate that


Take the Fuel return rail to a 5 litre Jerry can, apply air pressure to the FPR hose that goes to the inlet (push bike pump to around 10psi then run the pump, you should see it hold constant pressure to whatever it is set to.

I expect your pump is the issue, take it out and throw away as far as possible or vent your anger upon it with a lump hammer, make sure the new pump has good filters on both sides.

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jlayton

posted on 15/6/15 at 12:08 PM Reply With Quote
To use a external fuel pump I take it I have to remove the intank pump? How do I do it as its got all the std setup in the bottom of the tank
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MikeRJ

posted on 15/6/15 at 12:17 PM Reply With Quote
quote:
Originally posted by jlayton
I turbo'd it on completely std internals at 8 psi so yeah my own fault. but it lasted 4 hours on the rollers sweet as a nut. the thing on my mind is when it started running rough I thought id check the plugs, to my amazement they was not even hand tight (I mean really loose) and the washer on the plugs was not even squashed from new? would this of caused it to get 2 hot?


If spark plugs are not correctly torqued down then they will certainly run hotter since the thermal impedance between plug and head has been increased. This could potentially lead to pre-ignition and subsequent detonation if the engine was already on the edge. However, it seems more likely that the engine leaned out, and extreme detonation has caused the spark plugs to loosen (as well as destroying the rest of the engine).

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CosKev3

posted on 15/6/15 at 12:24 PM Reply With Quote
quote:
Originally posted by jlayton
To use a external fuel pump I take it I have to remove the intank pump? How do I do it as its got all the std setup in the bottom of the tank


If you don't want to change tank arrangment you will need to fit a swirl pot, then your standard pump would just be used to lift fuel from tank to swirl pot, then your new higher pressure pump would feed out of the swirl pot to the fuel rail.
pretty sure you would be best off feeding the return from the fuel reg into the swirl pot too.

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jlayton

posted on 15/6/15 at 12:30 PM Reply With Quote
I have a friend who's a great ally welder so prob better off modifying my tank for external pump by the sounds. Cars in pieces so no rush at the minute
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mark chandler

posted on 15/6/15 at 02:49 PM Reply With Quote
Swirl pot is best fed with a low pressure pump, just dump the in tank pump, extend the pickup rod to just above the floor and have a slot cut at the end so it cannot get blocked with a flat piece of rubbish.
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